Wednesday 9 November 2016

One more Step

Okay, I'm getting excited for the weekend. I really just can't wait for the wheels to lift off the ground and get that Sonex feeling again. My parts have all arrived today, and, earlier than expected.



Oil lines, Oil and the remote oil filter housing. I'll pick up an oil filter tomorrow and hopefully do this addition tomorrow after work. Double check everything on Friday then either fly Friday after work or Saturday. Well that's the plan anyway.

BACK IN BIZ BABY :)


Thursday 20 October 2016

Cowling vents and heat shields

So after melting various bits and bobs in the engine bay I finally installed some vents to vent the hot air after shutdown. I have not painted them yet but I think they look ok.



I was going to go to the trouble of sinking them in the cowling flush and so on but thought I'd trial them and maybe one day do that or probably just paint them first and fly till all the bugs are sorted. They are just a vent I bought on ebay, plastic and screwed onto the cowling. I have flown about 4 hours with these on and have noticed no change in engine temps during flight but after shut down, if you hold your hand over the vent, you can feel the hot air venting. This makes me smile.

Before I added these vents I had lots of trouble. I don't know if this caused the MGL RDAC to fail but I guess I'll never know.

I have also added some very crude looking (at this stage) heat shield over the engine mounts and trigger modules.





The heat shields are just made with some 6061 scrap I had and stainless zip ties and the insulation is a sticky backed  sheet that I have just stuck on and crudely moulded onto the accessory plate. I have also double wrapped the exhausts with two layers of exhaust wrap now too.  Since doing these small things my engine mounts have not needed changing and they seem to have stopped compressing even after the shortest of flights.


This pic shows the near new engine mounts after about 4 x hours flight. They had melted and crushed up and the pin was rubbing badly on the accessory plate. You can feel it in flight when they have worn or melted down as the engine begins to vibrate badly telling you that's the end of flying for that day mister.  Oh don't worry about the horrible brown leaks down the lower engine block, it's not oil , it's permatex from the initial engine build :)



 A vain attempt to add a washer or two to keep them tight, you can see how much the back one has compressed so I fitted a new front rubber and some washers to try and limp me through another flight.






Probably hard to see but the pin was rubbing on the accessory plate. New mount time again.



An indicator of how much it sagged as the prop rubbed on the cowling and scratched the paint,,, wasn't happy at all.


These lower three pics show the trigger modules and how much they had swollen up like balloons due to the heat from the turbo after shutdown, I assume, as inflight they have air running over them. I expect it was just the radiant heat when turned off cooking them or maybe in flight who knows. All I know is that since fitting the shield over the trigger modules they have stopped swelling. Both the top and bottom modules are swollen like this now but they aren't getting worse thankfully.  I emailed tech support early in the piece to ask about modules swelling up and was told I was the only one they had seen this happen to. As usual I guess I have done something wrong and not followed the instructions carefully enough. Anyway, it's fixed now. I will probably order 2 x new modules and another complete set of engine mounts and fit them so that now with the shielding in place the components should live long and happy lives in my cowling with the vents on the roof.

















It's been a while and I apologize for what you're about to read.

Yes it sure has been some time since posting on this blog last. A million and one things have happened and not all of them good.

 To take us up to where I am at this exact moment can be summed up with the one word "Grounded" .   I had been chipping away at the hours and now have about 17 or so. Sonex released a service bulletin regarding the turbo and what needs to be done. Essentially the bulletin requires the use of only one type of oil worldwide and of course it has to be a specialist oil only made in the great US of A. That's fine, however trying to get my hands on it is rather difficult. I had quickly found out no one from the US will post it like normal freight so I had to find a supplier in Australia that had already done the importing and buy it from them. All good, I found a place and ordered the oil. So one month later and numerous contact with the supplier had them realising it had been delivered to the wrong address and they couldn't get it back from that person. That's handy. They are now thankfully sending me out another batch and I should receive it in the next week or two.

In the meantime Sonex have released another bulletin requiring the addition of a remote mounted oil filter and a mod to the turbo drain line. So here I go again and no parts suppliers in Australia seem to have this component. I have sent away for the part and the due date is 16th November to land on my doorstep. So let's call this a 2 x month grounding. With the info being tossed around in regard to improvements and so on to avoid melting key components, I am assuming like MGL modules and Aeroconversion trigger modules and engine mounts etc, due to the massive heat soak after shutdown, Sonex are again looking at further improvements in design. With some luck I may be flying after christmas.

So that's that and where I'm at. My plane has been pushed into the corner.




My poor old plane, the Aeropup, has been through the wars of late too. I had a random person contact me about the plane who seemed to be extremely interested. So as one person was keen I thought I'd advertise it while I had some interest. Long story short two lots of different people were keen to look at the plane but as I had it at home where it can't be flown, they asked me to take it out the the airfield and carry out the 100 hourly and get it flying. Well I did all this including trailer hire, temporary hangarage, numerous costs for the annual and parts replacement due and of course avgas.





 So all flying well, took the missus for a fly, contacted the people to tell them it's ready to be viewed and guess what?.. Phones not being answered, txt messages not answered, emails not answered.  Very disappointed. I'm not disappointed about not selling the plane but just in the outright pricks for asking me to do all this work then not even giving me a return call. Anyway,,took the plane home and it can sit in my shed for another year or two as far as I'm concerned. If anyone now thinks they may be interested they can come to my house, view he plane, and if keen, hire a trailer and help me take it out to the field and then fly it. Won't likely happen but that's about all I can offer at the moment.




So okay I'm almost all done with the negative stuff but I do have to put just one more in. I'm certain I have definitely run over a black cat as on one of the last flights I had with the Sonex before the service bulletin releases I has a major leak sprout from the turbo feed line.






Oil had gone everywhere. I was luckily only 5 mins away from the airport when I smelt a massive stink of engine oil suddenly while flying. I made a lowish powered glide approach from about 6 miles out and watched the oil pressure gauge in case it dropped to nothing and landed all ok, taxied back and found thi(see pic).. Consequently I made a a new pipe that afternoon with the guys help from the club and had it running again. There was lots of discussion about how the pipe was unsuitable and so on, due to it being in a vibration high zone and things. Anyway the service bulletin now replaces that exact hose with flexible line so problem solved.

I did however have a bit of a win with some tyres. I was stuck on the ground for ages trying to sort out a tube for the wheels. I have since found out the tyre size is common in the US apparently yet not over here it seems. To cut a long story short I walked into my local tyre shop asking for tubes and he has some tyres there. They turned out to be the exact ones I needed for spares and a replacement. He wanted $50 a tyre. SOLD I said,,, The supplier I had talked to earlier that day could supply them each for $150 plus postage, WINNING,,, anyway another kind builder from over east sent me a second hand tube to get me flying again while I waited for the tubes to arrive for spares. Life was good again. He also sent me this jack for a very modest price. Lightweight and works great. Best thing I've seen for jacking up a plane that can store away for trips and is super light and easy to use. For anyone with a Sonex, I can't help but say this Jack is great.














Monday 11 July 2016

Down and out once again due to instruments

Seems instrument troubles are once again the order of business for me.  After the last flight I had, and being as happy as a proverbial pig in, you know what, my next attempt at flight turned to just that.  At 9.3 x hours I hopped in the plane, after a pre flight, and started up. I noticed the engine instruments all crossed out on the EFIS. It took a while and then they came to life. I was a bit worried so taxied to the main apron where they crossed out again. Hmm. Back to the hangar. I had just flown it for 3 hours or so that day and this was to be the final flight to take it up to the 10 hour mark for servicing. Anyway I looked over everything and all seemed fine. I had no idea what was going on. I jumped in the plane again and started up and all was working again. "What the Heck". So I carried out a short flight and brought the hours up to 9.7 total so close enough for the 10 x hour service.
 A little bit worried the next day about the going on's of the EFIS again I carried out the service on the engine and so on and powered up the Instruments. This time nothing was happening in regard to the engine instruments at all.  I carried out a very comprehensive check of the wiring with no faults found. I had noticed the steady flash of the green LED on the RDAC and was thinking that was a good sign as in the manual it says that's what they do. Well actually that's what they do when they aren't transmitting data it seems. When they do transmit, they have a nice data type random blinking pattern like you would see on a modem communicating. Had I known about this b4 it would have saved me a week of stuffing round.
So after a week of no results I rang the MGL dealer who was quite certain that the RDAC had  probably failed in some way and he would post me a replacement. I was VERY appreciative as I had lost a week's flying already and I should be flying again by next weekend. So I got to Friday and no module in the mail. Great... 2 x  weeks flying down the tube now. I rang again Tuesday thinking maybe it will arrive on Monday and I'm just being impatient. Nope, get hold of the Dealer, "oh sorry, I forgot to send it."  Typical, just my luck.
 Being the 3rd week now of no flying a shiney new RDAC arrives in an express post bag on the  Friday morning. "WOOHOO, flying this weekend".   Open the box, Wrong RDAC, Doesn't have a MAP sensor.  Let the swear words begin.  So on Sunday arvo I had calmed down enough and rang the Dealer again. He apologised and said he would send the correct part on Monday. Well hopefully he will and has, so I am patiently awaiting its arrival.

My last flight now was on the 11th of June, exactly one month ago as I write this. Massively disappointed in my choice of instruments and I don't know if I have just had a bad run or not but, in less than 10 x hours, I've needed a new EFIS and RDAC.  I am now really worried about the long term prospect of a reliable single glass panel dash. I should have added round dials and saved myself thousands and been flying still. I have been constantly trying to work out if I have done something wrong with the install or caused this issue somehow. I bought all the pre wired harnesses and followed every instruction to the letter, so that thought process has not really been helping. I have had very experienced people helping me out in the process and they all can't see an issue apparent in the install. So it looks to be a bad luck case for me once again. If I could do it over again I would have bought the whole instrument package with the airframe from SONEX .  In the US, there is a three year warranty on the instruments, here in OZ we only get one year.  Warranty time is quickly running out for me and I haven't even flown for ten hours yet!

Anyway I'm hoping the last of the problems are now behind me.


Sunday 12 June 2016

A New Dawn

Ok, so after today I have to admit I'm getting a fair bit excited about this plane. I am now trying to put all the negative behind me and focus on the future and I have to admit it looks good. I flew today  for 2.1 hours and started to do some general testing with speeds and fuel flow.  I started out flying over the airfield for 40 mins then, after it performed flawlessly, I ventured out of the proximity of the airfield and set sail.

Some very basic figures so far, that's if I can rely on the accuracy of the fuel flow metre, but here they are:
- 100kts @ 12.5 Lp/h
- 110kts @  15 Lp/h
- 130kts @  22 Lp/h
These figures were at about 4000 to 5000ft for reference.

I have noticed that on take off it is very easy to boost the heck out of this motor. I was a little bit tardy noticing today on take off when I saw 44" hg in the climb . It wasn't for long and I had only just gotten  airborne so backed off to about 36" and continued the climb out. It was a short runway and gusty so settled for 36" and climbed out at about 800 fpm. Temps have been fantastic since the addition of the Rotec tbi and the enlarged cooling outlet. Max temp on climb today I saw was about 380f on the hottest cylinder. Happy days for sure.

According to whatever you read the Aerovee is supposed to be broken in hard. Treat it mean keep it keen I believe. Well today that just wasn't going to happen. The turbulence was a huge limiting factor and mostly I was really only flying at around 2600rpm @ 24" map.  It was averaging about 110kts and that was about the top speed I was comfortable with. I'd like to think it will still be run in ok and upon landing the compressions felt really good turning the prop over so we will see.

I tried in vain to set the compass module for the discovery lite. It seems I got to 99.3% done but landed so will have to do it again I guess, I'm not sure why it wouldn't finalise but will read the instructions again and try next flight.

I have also today set the dial a trim correctly. I'm not sure why I didn't read the manual correctly but in doing so today I found it works perfectly and now flys very close to hands off. I also cut the trim tab down by half on the aileron but need again to trim some more off. It should be perfect after the next adjustment. In regard to the elevator trim I think I just erred on the side of caution in regard to the initial setting. I didn't want to find myself with a huge amount of up trim on the first flight so was a tad too cautious. After the adjustment today though all is good.

So for future flights now that the temps and engine seems under control I best start documenting the SAAA cards for the phase 2 registration. I have about 36 hours to go so need to get cracking. There seems to be a large number of them so time to start. They basically help you determine best glide speeds and climb stats so should be fun and also something to do to help pass the time for the test hours.

Some pics of today's flight







Sunday 5 June 2016

Ok who has a smile from ear to ear?

Well as it turns out ME !!!!!!!




I flew the plane today for a nice 0.7 flight and a now 2.1 hours in total. With a nice Carb fitted and good mixtures it climbed out with temps all in the green. The CHT's never exceeded 400f and it climbed out great. I took it up to about 5000 ft and circled the airfield before a quick fly over the house to wave to the wife and daughter as a sort of victory lap. I have to tell you I was very happy upon landing as the whole flight was perfect. Dodging a few low clouds here and there saw me level out and start to see some good numbers on the panel.






The 3rd pic is a bit hard to see but straight and level at about 29-30 " I was TAS about 129 kts. Sweeeeeet.   The first two screens I was on a gradual climb out of about 200-300 fpm.

I'm so far really happy about the performance. Hopefully after 20-30 hours the engine will cool down some more like they usually do. I have a good positive feeling about it all now and looking forward to seeing these 40 test hours behind me.

I added an aileron trim tab that seems to be a bit large now. At the faster cruise I was at today, now temps are under control, the wing wants to go the other way funnily. I will reduce the size of the tab next time I'm out at the field and that should sort that out. I believe I will also need to add some more spring tension to the elevator "dial a trim". I just can't seem to get enough up trim for any flight operation so far. I have been flying with full up trim for the whole flight so need to get onto that asap. It will be nice when it flies hands-free after being all set up properly. Now the engine is running like it should I can start to concentrate on those sorts of things.

So I only flew the 0.7 today but I think I will just do the first oil change after the engine rebuild now. This will see me able to fly off the next 5 hours before it's due again as part of the break in procedure.

 Happy days.











Fuel system makeover and engine rebuild.

Well its been a fair amount of work to get the plane back running again. I have been busy adapting the new Rotec tbi to the aircraft and doing a new fuel line system.  I have basically copied the fuel system off my other plane and fitted a one way valve and a fuel pump in parallel. Essentially it runs on gravity most of the time and the fuel pump can be used for takeoff and landing if desired and perhaps one day aerobatics.




There seems to be adequate clearance between my foot on the rudder pedals and all the components so hopefully all will be good. Obviously I still need to wire up the pump but I thankfully put all the wiring in place just in case long term I had to fit a pump. I honestly didn't think I would need to be fitting one at 1.4 hours but that's how it goes. 

I've had to make up all new controls, cable brackets and air cleaner spigots as well in the drawn out process of changing the carby over.  The new tbi also requires a primer so a 3rd cable was also required to be fitted to the aircraft. The controls were all ordered from Spruce and were here in a very short time after ordering. 



My dash looks a little like this now. Conventional throttle and mixture controls with an added 3rd cable for the primer. 





So it turns out I forgot to take photos of the brackets and spigot I had to make up to adapt this carb to the aerovee. You can see the TBI all fitted but the details of the brackets are a bit hard to see properly.   It all seems to work fine so a test flight I think won't be too far off.  I carried out a flight attitude gravity only fuel flow test after all the work was done just to be sure. Results were fine so not much to hold me back now. 

Let's hope this is the end of all the major issues and from now on it's all smooth sailing.  I'm really after that big grin after a successful flight. 









Monday 9 May 2016

Ups and downs,round and round

Okay beware everybody, a bit of a negative post coming up again, sorry.  I have to be honest, I have been having a really hard time with this plane.

Well I eventually had a win with the Instruments. The Australian dealer came to the party and sent me a new Discovery lite. Long story. Well I assume it was new as it had the plastic wrapper on the screen and looked good. When I powered the unit up it didn't seem to have the default screen and it had extra things on it loaded like a weight and balance chart for a different aircraft. It had a few things missing like the battery voltage and amp gauges. I was not too worried as I could just load the old screens from my memory card that I saved them all to. So I go to load the screens on and guess what?! I cant't find the memory card. To say I searched high and low to find this card was an understatement. I looked everywhere. I did find some odd things searching through all my cupboards and so on as you do but no micro sd card. At a huge loss I rang the Australian dealer again who was away at the time. A few days later I got in touch with him again when he was home and he told me the card was in the old unit. Damn, I can't believe I was that silly to leave it in the EFIS. Oh well. He said he would post it no problems but I happened to ask if he could send the files via email if that was easier. "Yep, No Problem. I'll do it within the hour" So weeks later the email still hasn't come. I give up on that front as it's just too hard. It took me hours and hours to set the screens up again manually and basically I can only blame myself.  I did fly the plane again and "YES" everything works fine. I was so relieved and felt that little bit of a smile creep in. What was not good however still was the engine temps. Sky high once more but at least I could land with an ASI that was working and a fully functioning EFIS.


I had played with the mixtures again on the Aerocarb and tried to richen the baby up some more. It got to the point now where starting the engine was finicky as if I didn't have the mixture right it would flood and carry on. Still determined to get it right I flew it again. Temps still high. After scouring the forums I just decided to do what most builders do and open up the lower cowling. I cut out an extra 2 inches for a total of 6" x 13" lower outlet. I reinstalled the deflector lip and flew the plane. As per the video Below I flew the plane and the CHT's were drastically lower and all under 400f. WINNING.  The EGT's were a little high and I gave the carb a tickle richer and flew the plane again. Honestly thinking this was finally going to be my victory flight I was soon to be proven wrong. I took off and instantly noticed the mixtures were drastically wrong and I was in trouble. I felt the power loss in flight and carried out a very small low level circuit. Landed and taxied back to this.







It has spewed a massive amount of oil out the front prop hub and oil was everywhere and almost back to the tailwheel. I was soooo stoked I just wanted to give up.  Turning the motor over by the prop indicated 2 cylinders had no compression.

I pulled the motor down the next day and discovered the two rear cylinders had issues. One side had a leaking exhaust valve and the other side has a melted piston, snapped ring and a stuffed barrel.








One thing that is an absolute bonus about this engine is the price of parts and the availability. I had the heads tested and all 8 valves and seats re-ground. This cost me $125 at the local automotive machine shop. New piston rings cost me $124.50. I happened to have 2 x good condition second hand barrels from the first engine rebuild on the other Aerovee so that was good. I used one of the cylinders and pistons so I still have one good one spare in case I ever need it.  I then went and ordered a Rotec Tbi to avoid destroying another engine by running excessively lean mixtures!

I reassembled the engine yesterday and ran it for the last time on the Aerocarb. I didn't run it for long and only just long enough to make sure it was okay and running fine with no abnormal noises etc.  It ran fine and again a little smile crept in.

Today I started to carry out the Rotec Tbi conversion. I plan to get it mounted and running first just on gravity feed then decide about the boost pump. I took the old aerocarb off and set about making the brackets and so on for the cable attachments and additional primer set up. I am still dismayed by the lack of anything supplied for brackets or any forms of mounts especially for the air cleaner side. Talking to the factory regarding this was fruitless so I need to make them myself.  I really love the way the engine runs on the other plane with the Rotec Tbi so I guess I can put up with the lack of support and just forge on. I would like to add a fuel pump eventually as I noticed on the other plane the mixture control seems nicer for want of a better word to describe it. It just has a better feel. The other plane I can run gravity or the fuel pump as it has a one way valve and an alternate path for the fuel for gravity feed. It's still a pain on both as with the fuel pump on the fuel flow meter reads higher than what it is really using, I think due to the pulses from the pump. If I run gravity feed the fuel flow reads accurately but the mixture doesn't feel as linear. So we'll see when I get it running what I do long term.


Please bare in mind that this video is just my twisted thoughts on the matter. . Don't let my grumblings persuade you one way or the other in what carb or system you think is better. I'm still trying to get over the fact I'm rebuilding my engine one hour into the test flight phase. I'm actually wondering if this is some kind of record!








Monday 4 April 2016

Instrument woes and overheating

Well I now have a total of four flights on the scoreboard and one hour on the grand total.  Achieving these milestones has been exactly that too. From the first flight I have been battling sky high temps and Instrument problems. My plan has been to try to get into the air asap after startup. Obviously though with common sense I have carried out all the pre flight checks and run ups and so on but I just haven't dawdled. I have attempted to climb out with moderate power until the temps max out then lower the nose and maintain height or do an ever so slight climb to try to keep the temps under control. Any attempt to speed up for more airflow results in a roasting motor again. On the longest flight of 35 mins or so I was maintaining about 4000 ft and temps were okay at about half throttle. Trying to get to a decent cruise setting sent them upward once more.

The MGL instruments I must say have been the biggest disappointment so far however. On the first flight my ASI was okay. On the second flight it decided to stop working. "Great" I thought, it was reading 70 kts and was stuck on that. I cycled the power to the efis thinking maybe it might just work for me again. Nope, and now it just read 0 kts,,, great.... so I chose not to panic and carried on as usual and made my base and finals approach nice and hot with plenty of wind noise over the canopy. Rounding out and touching down just fine.  I set about finding the issue with the EFIS. I have been over the wiring with a fine tooth comb. Every wire, power,earth and plug has been pulled apart and inspected and tested with my multimeter whist giving a good twist and so on to try and replicate the issue.  I had noticed that the local time had kept needing to be set so figured that the memory battery being flat could somehow contribute to this. I changed the battery and refitted the EFIS. With gentle wiggling of the wiring I had a solid reading for the ASI and thought I must have it sussed. I flew the plane again and YEP no ASI again. Getting really frustrated with this I landed. Bare in mind while I keep losing my ASI and causing stress I seriously don't need I am also battling the overheating issues to top it all off. Quite a recipe for disaster If I don't say so myself. Before this flight I had modified the Cowling inlets and Outlets as Per instructions from Sonex. I had also done the mod to the heads in regard to opening up all the airways around the exhaust ports and in between the 2 cyls on the heads like perhaps others have seen pics of  before.




All these passages have now been opened right up for added airflow. I wish I had taken some photo's of them opened up but I can do that next time I am at the airport.





These pics are a bit of a before and after in regard to the cowling Lip added. It is basically 2" long over the original 1" long and has the tapered sides as well.  On the last flight I did I saw 390 f on three cylinders and the one cylinder still skyrocketing up and over 450 f.  I seriously think I have run over a black cat that was pregnant with thirteen black kittens. The mods certainly have reduced three of the CHT's , I just wish all four had been okay.  I have also been playing around with the baffle seals a little and replaced a section that was in three pieces with a singular piece in the hope the air has not been bypassing the joins. I have also spent some time just trying to work out why 1 x CHT would  be so much different. The sensors all read the same when turned off and warming up. It's just when I get airborne one heats right up.

I am hesitant to modify anything now while I have no Instrument and flying obviously is not going to happen so I now just need to sit on my hands and wait.

I rang the Australian Dealer for MGL and asked how he was progressing with the checking of the ASI and EFIS in general.  It seems highly likely now that it will be heading off to South Africa for a proper test. I honestly wonder what next. I am thankful it is still in Warranty having only bought the whole system around 10 months ago. Let's see what comes of the testing and progress from there. I mostly bought a MGL system as my original one in the Aeropup has performed flawlessly from day one. I fully expected the second system to be the same in terms of reliability but perhaps I was just unlucky.

Well sorry everyone for such a negative update. If I can get on top of these two issues I think it will then be smooth sailing. I am just a little frustrated that's all due to the fact that I have to fly forty hours in one calendar year to finish the test hours off or I have to go through the whole registration process again including all registration and inspections costs so the clock is ticking. Secondly winter is fast approaching and right now almost to the day the best weather for the flying season is upon me. Calm winds, blue skies and no big thermals inland. With the EFIS heading to South Africa most likely I will be grounded for a Month at best guess. Time to twiddle some thumbs.
















Tuesday 22 March 2016

The culprit

Back in biz it seems after a short delay.

I managed to change the coil out and back in business I was. It's hard to imagine a part failing so early in the programme and I was a little worried I had misdiagnosed or made an error somewhere. It turns out I worried over nothing and it's all good now. The coil had a few slightly different markings but was identical in all major aspects so I bolted it on and gave it a whirl. The engine fired up and ran great on both ignitions. Happy days once more. Now to just sort out this overheating issue.



This was the little bad boy here. I should just throw it straight in the bin but I think I want too look at it for a little bit longer in disgust, then chuck it away.


Thursday 17 March 2016

First flight video



Unedited video from the first flight. We had a proper video camera on the day and completely forgot to use it in all the excitement.  Mobile phone video was all we managed to obtain.









First flight

Well I can officially say I have flown the plane !!!!!





It didn't go quite according to plan but nonetheless it was a good outcome. I have to say I was very nervous before the event. I ended up with quite a crowd which was not ideal but expected.



I did have on hand one man on the ground who was my emergency situation guy. He had the car airside, handheld radio and a few different fire extinguishers just in case the worst happened. I just felt better knowing he was ready and close by. Not that either of us thought anything would happen, still we just wanted to play it as safe as we could.


After a good clean of the windscreen (as you would be amazed how much dust can accumulate) I was taxiing for runway 21. There was lots of talk of this and that and people giving advice which I respectfully didn't want to hear as I had my plan in my head of the flight and that's what was going to happen and did happen, to a degree.



I had an issue with the ASI at one stage and I hadn't seen a reading on the dash in this regard during the taxi out and line up. I made the decision and taxied back to double check it. As luck would have it it was fine but I felt better checking.

 I strapped in again and set off once more for runway 21. Another aircraft was in the circuit, as it happens a good friend so he extended downwind and I lined up. Radio call made, accelerated and it just seemed to leap off the ground like a jack rabbit. I climbed out watching airspeed, climb rate and the CHT's passing into the yellow. I was at about 33" manifold setting and climbing out at 85-90 kts in  a very shallow climb to increase airflow. I then saw the gauge hit the red and leveled out for a 500 ft circuit. Throttled back on a short crosswind and turned downwind on a very low power setting. I was throttled right back and seeing 95-100 kts. The gauge began then finally to drop somewhat and turning base called and final right after for a very bunched up circuit. I was very high at 500ft for the markers so landed about 1/3 of the 2km runway down. Touchdown was perhaps not ideal as it felt like the tailwheel definitely touched first then the mains. It was a event free landing so taxied back to the hangar for a total of 6 mins flight.  That also was my first ever flight in a Sonex.

I had known almost from about 100-200 ft I had the engine set too lean. It heated up way too fast and I knew I was going to have to get back quick. I had heard all the reasons why builders shouldn't test fly their own planes and so on as if there is a problem that they will try and save the plane and not themselves, well I don't think that is the case with me. I don't think I am that attached to it. From all the flying I had done in the other Aerovee I knew the temps and so on and flew accordingly and not dangerously I feel. I have always practiced low level circuits so there was a good reason to do one with this Sonex.

Back on the ground and a while later I took the cowl offs and richened up the Aerocarb. I was quite ashamed of myself by how much I had actually had to richen it. I think the next flight will be ok now the engine is getting a heap more fuel. It made a big difference on the last plane so am sure it will make a big difference on this one too.

I was about to go fly the plane again and when I carried out a Mag check found I was running on 2 cylinders only on the primary ignition. Figuring I had melted some ign leads or something I took the cowls off again and everything looked ok. I had found which cylinders weren't firing as the EGT's dropped significantly on number 3-4. Well actually number 1 and 2 but I am a little bad and number my cylinders on the efis the opposite way as it just seems to make sense to me. Anyway the lower coil wasn't firing. I took the cut off wire off and tried again. No change. I took the plugs out and changed them. No change. I checked the coil with a multi meter and compared it to the top coil but it seemed the same. I checked to make sure the coil had the additional earth and that it was ok. No change.  I closed the hangar doors and gave up.

Somewhat very despondent I looked up the Sonex site and thought about how long now I was going to be grounded waiting for parts from the US and the cost. I looked up the builders website and saw the number for the replacement coils from a local mower shop. I cross referenced the numbers here in OZ and my brother ordered me one via his work that specializes in this industry.  The coil as it turns out arrived today in the post. It looks the same as the original from memory and I will change it out tomorrow and see if the engine runs again on the primary ign.  It was about 1/3 price total delivered if I take into account the foreign exchange and freight. I like to support Sonex but can't justify the time and cost on this one. A failed coil after 6 mins flight is infuriating. I am not blaming Sonex as it is in no way their fault but still frustrating to have a failure of such a new part.

The weather is looking great for flying on the weekend so if all goes well I will be reporting some fine flights very soon. I also want to change the needle to a number 3 from a number 2 in the Aerocarb so that may happen this weekend too.

Oh I almost forgot to tell you how it flies :)

 Well..........

  Downwind was about the only time I got to semi relax. It seems quite touchy in the pitch and the roll is quite responsive too. It has the extended ailerons so putting it down to that. I had to hold a bit of right aileron to keep it level so will need to add a trim tab of sorts. I didn't have enough time to really get a feel for the vision over the screen but it seems a good forward visibility is attained in cruise. I was all over the place in regard to height and I did try somewhat woefully to try and trim it out with the dial a trim. The trim worked fine but I just didn't have time to look at the dash and fly and set up for landing so that's a job for another day.  I am happy by the way it flew and think it will be a really nice plane once I get some time on the Hobbs.